thanks for that info.
i bent up the bundy to fit without the banjos. kinda bummed me out, 'cause it had come out looking good.
now it looks like bent-up bundy.
mabe when i do the remote reservoir i will revisit this, but i am still mostly looking for function.
brakes seemed to bleed well again, and no leaks that i can find.
rotating equipment in the "shop" again- moved the tire "machine" in place for use.
i want to get it off these blocks.
abitl8tr
got the wheels on and removed the blocks.
dug up some garden for honey and fixed some fence.
lakoftime051815
seem to have some clutch, but have only found some forward gears so far. seems the shift linkage is stiffly loose.
also seems the fuel pump is spitting gas, so i didn't run it long.
the exhaust thing i cobbled together made it a bit quieter.
perhaps some road testing will happen next month.
i think i will register it.
cuplminuts052015
poking into the fuel pump a bit has me making a block-off plate, and going electric.
the existing carburetor has a leaky float valve (again). time for replacement, and it's time to get some throttle control.
charging system stopped charging for some reason that is probably my fault.
all is good and shaking out will continue in spurts. built more fence around the compound. still putting the steady in at the salt mine, also.
mordun052215
timeoff from the grind, so i swapped out the weber32dfm with a weber32/36dgv.
installed a pressure bleed with an early jeep fuel filter(wix33040) that i still need to figure out where/how to mount, and a little 3-5psi electric buzz pump.
still need to pull the ruptured mechanical pump and blind off that hole, but ran it for a while, and it sounds pretty good.
still need to put the steering wheel back on and find a reverse gear..............
smxtratime052315
a few minutes to install steering column/wheel, and some consideration for control of the carburetor...... visited a bicycle shop, but found no inspiration. checked a motorcycle shop with same results.
canthelpit052515
hung the flag out at half mast, did some yard work, watched the ball game, snuck in some europatime and tried some control cables for choke and throttle.
perhaps i have found where that reverse gear is, but i still need to look into the shift linkage- that center bunch is real sloppy. seems to have lots of play in some heim(?) joints.
mabe when my wife is done with an after giants game siesta, a movement test will happen. think it may kinda work........should be interesting.
testreport052615
moved around the driveway a bit. unsure about clutch, but can't find gears well enough to really tell what's happening.
several pieces of the shift linkage have been repaired with a welder, but now the relay lever ball joints aren't replaceable anymore.
parts is parts, and i decided to throw some money into linkage parts, so parts are being ordered.
had to report for duty this am- still the wage slave.